Form 21 | Related Doc | Date Submitted: | 6/2/2022 | MIT Assigned By: | | Date Recv'd: | 6/2/2022 | Facility ID: | | DocNum: | 403066792 | Facility Status: | | Operator Information: | Oper. No. | 16700 | Operator: | CHEVRON USA INC | Address: | 760 HORIZON DRIVE STE 401 GRAND JUNCTION CO 81506 | Type Of Facility: | | Well Status: | Facility Name | UNION PACIFIC | Operator contact: | Anita Sanford | Location: | | qtrqtr: | section: | township: | range: | meridian: |
| MIT Details: | Test Type: | VERIFICATION OF REPAIRS | Repair Type: | | Repair Desc: | Isolate a casing leak from 3951 – 4668’. Cement squeeze, fished injection packer and mandrel system down to 6,183’. Acidize, Isolate casing leak to two intervals from 4,594’-4,692’ and 4,952’ – 5,179’ Cement Squeeze. c/o, new packer and tubing. | Test Date: | 6/1/2022 | Field Rep: | Browning, Chuck | Approved Date: | 6/6/2022 | Approved by: | | Last Approved MIT: | 7/3/2018 | Injection/Producing Formation Zones: | WEBR | Perforation Interval: | 5831-6436 | Open Hole Interval: | | Bridge/Cement Plug Depth: | | Tubing Size: | 2.875 | Tubing Depth: | 5739 | Top Packer Depth: | 5651 | Multiple Packers: | | | Condition of approval: | | Test Data: | Wellbore Channel Test: | Reading Type | Pressure | 10 MIN CASE | 1250 | 5 MIN CASE | 1250 | FINAL CASE | 1250 | START CASE | 1250 |
| No channel test. |
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