Form 21 | Related Doc | Date Submitted: | 7/22/2009 | MIT Assigned By: | KRABACHER, JAY | Date Recv'd: | 7/24/2009 | Facility ID: | 150200 | DocNum: | 1171079 | Facility Status: | AC | Operator Information: | Oper. No. | 16700 | Operator: | CHEVRON U S A INC | Address: | 6001 BOLLINGER CANYON RD SAN RAMON CA 94583 | Type Of Facility: | UIC ENHANCED RECOVERY | Well Status: AC | Facility Name | LEVISON | Operator contact: | DIANE PETERSON | Location: | | qtrqtr: SENE | section: 16 | township: 2N | range: 103W | meridian: 6 |
| MIT Details: | Test Type: | VERIFICATION OF REPAIRS | Repair Type: | OTHER | Repair Desc: | plug set in profile, perf. tubing, circ. packer fluid, re-tested casing integrity. verifies that well has tubing leak, (not casing) will remain shut-in and on work-schedule to have tubing replaced | Test Date: | 7/14/2009 | Field Rep: | | Approved Date: | 7/24/2009 | Approved by: | KRABACHER, JAY | Last Approved MIT: | 5/3/2004 | Injection/Producing Formation Zones: | WEBR | Perforation Interval: | NA | Open Hole Interval: | 6172 - 6785 | Bridge/Cement Plug Depth: | | Tubing Size: | 2.875 | Tubing Depth: | 6422 | Top Packer Depth: | 6047 | Multiple Packers: | Y | | Condition of approval: | | Test Data: | Wellbore Channel Test: | Reading Type | Pressure | 10 MIN CASE | 810 | 5 MIN CASE | 825 | CASE BEFORE | 0 | FINAL CASE | 800 | FINAL TUBE | 0 | INITIAL TUBE | 0 | LOSS OR GAIN | -40 | START CASE | 840 |
| No channel test. |
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