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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-09236EMERALD
31AX
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
3/1/2019
RANGELY
72370
RIO BLANCO  103
NWNW 30 2N102W 6
315788View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:4/28/2005MIT Assigned By:KRABACHER, JAY
Date Recv'd:7/21/2005Facility ID: 150200
DocNum:1170762Facility Status:AC
Operator Information:
Oper. No.16700
Operator:CHEVRON PRODUCTION COMPANY
Address:100 CHEVRON RD  RANGELY  CO 81648
Type Of Facility:UIC ENHANCED RECOVERYWell Status: AC
Facility NameEMERALD
Operator contact:DIANE  PETERSON
Location:  qtrqtr: SENE section: 16 township: 2N range: 103W meridian: 6
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:TUBING/PACKER LEAK
Repair Desc:
Test Date:4/26/2005
Field Rep:
Approved Date:7/21/2005
Approved by:KRABACHER, JAY
Last Approved MIT:5/4/2004
Injection/Producing Formation Zones:WEBR
Perforation Interval:5712 - 6318
Open Hole Interval:NA
Bridge/Cement Plug Depth:
Tubing Size:2.875
Tubing Depth:5603
Top Packer Depth:5558
Multiple Packers:N
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE760
5 MIN CASE760
CASE BEFORE0
FINAL CASE760
FINAL TUBE0
INITIAL TUBE0
LOSS OR GAIN0
START CASE760
No channel test.