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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-06420MCLAUGHLIN, A C
56X
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
2/2/2023
RANGELY
72370
RIO BLANCO  103
SESW 14 2N103W 6
314697View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:9/20/1999MIT Assigned By:ADKINS, JAIME
Date Recv'd:4/25/2003Facility ID: 150200
DocNum:893632Facility Status:AC
Operator Information:
Oper. No.16700
Operator:CHEVRON U S A INC
Address:P O BOX 4791  HOUSTON  TX 77210-4791
Type Of Facility:UIC ENHANCED RECOVERYWell Status: AC
Facility NameMCLAUGHLIN, A C
Operator contact: 
Location:  qtrqtr: SENE section: 16 township: 2N range: 103W meridian: 6
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:TUBING/PACKER LEAK
Repair Desc:REPAIRED PARTED TAIL PIPE
Test Date:9/14/1999
Field Rep:
Approved Date:10/21/1999
Approved by:ADKINS, JAIME
Last Approved MIT:6/8/1998
Injection/Producing Formation Zones:WEBR
Perforation Interval:NA
Open Hole Interval:6260-6578
Bridge/Cement Plug Depth:NA
Tubing Size:2.875
Tubing Depth:6549
Top Packer Depth:6081
Multiple Packers:N
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE800
5 MIN CASE800
CASE BEFORE
FINAL CASE800
FINAL TUBE0
INITIAL TUBE0
LOSS OR GAIN0
START CASE800
No channel test.