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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-06259FEE
48
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
10/17/2022
RANGELY
72370
RIO BLANCO  103
NWSE 31 2N102W 6
314640View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:7/7/1998MIT Assigned By:ADKINS, JAIME
Date Recv'd:4/28/2003Facility ID: 150200
DocNum:622951Facility Status:AC
Operator Information:
Oper. No.16700
Operator:CHEVRON U S A INC
Address:P O BOX 4791  HOUSTON  TX 77210-4791
Type Of Facility:UIC ENHANCED RECOVERYWell Status: AC
Facility NameFEE
Operator contact: 
Location:  qtrqtr: SENE section: 16 township: 2N range: 103W meridian: 6
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:TUBING/PACKER LEAK
Repair Desc:& ADDED PERFS
Test Date:6/29/1998
Field Rep:
Approved Date:7/24/1998
Approved by:ADKINS, JAIME
Last Approved MIT:5/17/1995
Injection/Producing Formation Zones:WEBR
Perforation Interval:5744 - 6138
Open Hole Interval:NA
Bridge/Cement Plug Depth:
Tubing Size:2.875
Tubing Depth:6115
Top Packer Depth:5525
Multiple Packers:Y
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE860
5 MIN CASE860
CASE BEFORE0
FINAL CASE860
FINAL TUBE0
INITIAL TUBE0
LOSS OR GAIN0
START CASE860
No channel test.