Form 21 | Related Doc |
Date Submitted: | 3/22/2024 | MIT Assigned By: | |
Date Recv'd: | 3/22/2024 | Facility ID: | |
DocNum: | 403728560 | Facility Status: | |
Operator Information: |
Oper. No. | 10779 |
Operator: | SCOUT ENERGY MANAGEMENT LLC |
Address: | 13800 MONTFORT DRIVE SUITE 100 DALLAS TX 75240 |
Type Of Facility: | | Well Status: |
Facility Name | FEE |
Operator contact: | Anita Sanford |
Location: | | qtrqtr: | section: | township: | range: | meridian: |
|
MIT Details: |
Test Type: | VERIFICATION OF REPAIRS |
Repair Type: | |
Repair Desc: | UIC Failure post workover, well was shut in for high casing pressure. Pulled top packer, ran new top packer with FL injection string. Return to injection upon approval of a Form 21.
|
Test Date: | 3/21/2024 |
Field Rep: | Browning, Chuck |
Approved Date: | 3/25/2024 |
Approved by: | |
Last Approved MIT: | 9/20/2023 |
Injection/Producing Formation Zones: | WEBR |
Perforation Interval: | 6003-6465 |
Open Hole Interval: | |
Bridge/Cement Plug Depth: | |
Tubing Size: | 2.875 |
Tubing Depth: | 5984 |
Top Packer Depth: | 5766 |
Multiple Packers: | |
|
Condition of approval: |
|
Test Data: | Wellbore Channel Test: | Reading Type | Pressure | 10 MIN CASE | 1350 | 5 MIN CASE | 1360 | FINAL CASE | 1350 | LOSS OR GAIN | -10 | START CASE | 1360 |
| No channel test. |
|
|
|
|