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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-06141FEE
43
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
9/1/2023
RANGELY
72370
RIO BLANCO  103
SENW 19 2N102W 6
314569View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:3/22/2024MIT Assigned By:
Date Recv'd:3/22/2024Facility ID: 
DocNum:403728560Facility Status:
Operator Information:
Oper. No.10779
Operator:SCOUT ENERGY MANAGEMENT LLC
Address:13800 MONTFORT DRIVE SUITE 100  DALLAS  TX 75240
Type Of Facility:Well Status: 
Facility NameFEE
Operator contact:Anita  Sanford
Location:  qtrqtr:  section:  township:  range:  meridian: 
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:
Repair Desc:UIC Failure post workover, well was shut in for high casing pressure. Pulled top packer, ran new top packer with FL injection string. Return to injection upon approval of a Form 21.
Test Date:3/21/2024
Field Rep:Browning, Chuck
Approved Date:3/25/2024
Approved by:
Last Approved MIT:9/20/2023
Injection/Producing Formation Zones:WEBR
Perforation Interval:6003-6465
Open Hole Interval:
Bridge/Cement Plug Depth:
Tubing Size:2.875
Tubing Depth:5984
Top Packer Depth:5766
Multiple Packers:
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE1350
5 MIN CASE1360
FINAL CASE1350
LOSS OR GAIN-10
START CASE1360
No channel test.