Skip to Main Content

Incident Search

COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-07022HAGOOD L N
A-9X
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
2/1/2023
RANGELY
72370
RIO BLANCO  103
SWSE 23 2N103W 6
314706View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:1/27/2022MIT Assigned By:
Date Recv'd:1/27/2022Facility ID: 
DocNum:402939189Facility Status:
Operator Information:
Oper. No.16700
Operator:CHEVRON USA INC
Address:760 HORIZON DRIVE STE 401  GRAND JUNCTION  CO 81506
Type Of Facility:Well Status: 
Facility NameHAGOOD L N
Operator contact:Anita  Sanford
Location:  qtrqtr:  section:  township:  range:  meridian: 
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:
Repair Desc:HIGH CASING PRESSURE THIS INJECTION WELL WAS SHUT IN 08/10/2021 FOR HIGH CASING PRESSURE WHILE ON INJECTION. The workover consisted of pulling the injection tubing, and both the top & bottom packers, perform clean out, ran injection string and packers replacing packers, and adding a TM-40 spool & hanger. Open Hole 6485-6600
Test Date:1/26/2022
Field Rep:Browning, Chuck
Approved Date:1/27/2022
Approved by:
Last Approved MIT:7/14/2021
Injection/Producing Formation Zones:WEBR
Perforation Interval:6315-6459
Open Hole Interval:
Bridge/Cement Plug Depth:
Tubing Size:2.875
Tubing Depth:6286
Top Packer Depth:6221
Multiple Packers:
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE1250
5 MIN CASE1250
FINAL CASE1250
START CASE1250
No channel test.