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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-06306WEYRAUCH
2-36
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
2/1/2022
RANGELY
72370
RIO BLANCO  103
NWNE 36 2N102W 6
314665View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:1/17/2022MIT Assigned By:
Date Recv'd:1/17/2022Facility ID: 
DocNum:402928290Facility Status:
Operator Information:
Oper. No.16700
Operator:CHEVRON USA INC
Address:760 HORIZON DRIVE STE 401  GRAND JUNCTION  CO 81506
Type Of Facility:Well Status: 
Facility NameWEYRAUCH
Operator contact:Anita  Sanford
Location:  qtrqtr:  section:  township:  range:  meridian: 
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:
Repair Desc:The workover consisted of pulling the injection tubing and both top & bottom packers, performed clean out, ran injection string and packers, replacing upper packer and tubing and adding a TM-40 spool and hanger.
Test Date:1/14/2022
Field Rep:Browning, Chuck
Approved Date:1/18/2022
Approved by:
Last Approved MIT:4/6/2018
Injection/Producing Formation Zones:WEBR
Perforation Interval:
Open Hole Interval:6075-6486
Bridge/Cement Plug Depth:
Tubing Size:2.875
Tubing Depth:6007
Top Packer Depth:5894
Multiple Packers:
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE1250
5 MIN CASE1250
FINAL CASE1250
START CASE1250
No channel test.