Skip to Main Content

Incident Search

COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-08612FEE
53AX
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
2/1/2020
RANGELY
72370
RIO BLANCO  103
NWSW 22 2N102W 6
315502View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:11/4/2019MIT Assigned By:
Date Recv'd:11/4/2019Facility ID: 
DocNum:402230379Facility Status:
Operator Information:
Oper. No.16700
Operator:CHEVRON USA INC
Address:100 CHEVRON USA INC  RANGELY  CO 81648
Type Of Facility:Well Status: 
Facility NameFEE
Operator contact:Anita  Sanford
Location:  qtrqtr:  section:  township:  range:  meridian: 
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:
Repair Desc:Clean out, drilled through CIBP and Resin; reperforated and set top and bottom packers. Well to be return to active injection upon Form 21 approval.
Test Date:10/31/2019
Field Rep:Browning, Chuck
Approved Date:11/22/2019
Approved by:
Last Approved MIT:4/13/2016
Injection/Producing Formation Zones:WEBR
Perforation Interval:6270-6574
Open Hole Interval:
Bridge/Cement Plug Depth:
Tubing Size:2.875
Tubing Depth:6016.7
Top Packer Depth:5942.5
Multiple Packers:
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE1270
5 MIN CASE1280
FINAL CASE1260
LOSS OR GAIN-40
START CASE1300
No channel test.