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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-08103EMERALD
69X
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
1/3/2020
RANGELY
72370
RIO BLANCO  103
SWNW 30 2N102W 6
311819View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:10/28/2013MIT Assigned By:Covington, Dave
Date Recv'd:10/28/2013Facility ID: 150200
DocNum:2125000Facility Status:AC
Operator Information:
Oper. No.16700
Operator:CHEVRON PRODUCTION COMPANY
Address:100 CHEVRON RD  RANGELY  CO 81648
Type Of Facility:UIC ENHANCED RECOVERYWell Status: AC
Facility NameEMERALD
Operator contact:DIANE  PETERSON
Location:  qtrqtr: SENE section: 16 township: 2N range: 103W meridian: 6
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:TUBING/PACKER LEAK
Repair Desc:Changed out tubing and packer
Test Date:10/28/2013
Field Rep:Covington, Dave
Approved Date:10/28/2013
Approved by:Covington, Dave
Last Approved MIT:12/16/2010
Injection/Producing Formation Zones:WEBR
Perforation Interval:5628-6482
Open Hole Interval:NA
Bridge/Cement Plug Depth:NA
Tubing Size:2.875
Tubing Depth:6562
Top Packer Depth:5270
Multiple Packers:Y
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE1165
5 MIN CASE1180
CASE BEFORE0
FINAL CASE1150
FINAL TUBE0
INITIAL TUBE0
LOSS OR GAIN-50
START CASE1200
No channel test.