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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-08103EMERALD
69X
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
1/3/2020
RANGELY
72370
RIO BLANCO  103
SWNW 30 2N102W 6
311819View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:12/16/2010MIT Assigned By:KOEHLER, BOB
Date Recv'd:1/6/2011Facility ID: 150200
DocNum:1771070Facility Status:AC
Operator Information:
Oper. No.16700
Operator:CHEVRON USA INC
Address:100 CHEVRON ROAD  RANGELY  CO 81648
Type Of Facility:UIC ENHANCED RECOVERYWell Status: AC
Facility NameEMERALD
Operator contact:DIANE L  PETERSON
Location:  qtrqtr: SENE section: 16 township: 2N range: 103W meridian: 6
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:CASING LEAK
Repair Desc:Squeeze casing leak (Form 5 submitted), run new tubing.
Test Date:12/16/2010
Field Rep:
Approved Date:1/6/2011
Approved by:KOEHLER, BOB
Last Approved MIT:5/24/2005
Injection/Producing Formation Zones:WEBR
Perforation Interval:5628-6482
Open Hole Interval:NA
Bridge/Cement Plug Depth:NA
Tubing Size:2.875
Tubing Depth:6562
Top Packer Depth:5466
Multiple Packers:Y
 
Condition of approval:
Chart reads above 900 psi and is very consistent.
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE
5 MIN CASE
CASE BEFORE
FINAL CASE810
FINAL TUBE
INITIAL TUBE
LOSS OR GAIN0
START CASE810
No channel test.