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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-06167UNION PACIFIC
56-21
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
11/8/2022
RANGELY
72370
RIO BLANCO  103
SENE 21 2N102W 6
314590View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:4/11/2013MIT Assigned By:BROWNING, CHUCK
Date Recv'd:4/16/2013Facility ID: 150200
DocNum:1171473Facility Status:AC
Operator Information:
Oper. No.16700
Operator:CHEVRON PRODUCTION COMPANY
Address:100 CHEVRON RD  RANGELY  CO 81648
Type Of Facility:UIC ENHANCED RECOVERYWell Status: AC
Facility NameUNION PACIFIC
Operator contact:DIANE  PETERSON
Location:  qtrqtr: SENE section: 16 township: 2N range: 103W meridian: 6
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:TUBING/PACKER LEAK
Repair Desc:CLEAN OUT. REPLACE TUBING & PACKER
Test Date:4/11/2013
Field Rep:BROWNING, CHUCK
Approved Date:4/11/2013
Approved by:BROWNING, CHUCK
Last Approved MIT:6/6/2011
Injection/Producing Formation Zones:WEBR
Perforation Interval:6245-6486
Open Hole Interval:NA
Bridge/Cement Plug Depth:
Tubing Size:2.85
Tubing Depth:6480.7
Top Packer Depth:5998
Multiple Packers:Y
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE1180
5 MIN CASE1185
CASE BEFORE0
FINAL CASE1175
FINAL TUBE0
INITIAL TUBE0
LOSS OR GAIN-15
START CASE1190
No channel test.