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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-01060RECTOR
3
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
1/29/2016
RANGELY
72370
RIO BLANCO  103
SWSE 34 2N102W 6
314264View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:5/16/2007MIT Assigned By:KRABACHER, JAY
Date Recv'd:6/18/2007Facility ID: 150200
DocNum:1170981Facility Status:AC
Operator Information:
Oper. No.16700
Operator:CHEVRON PRODUCTION COMPANY
Address:100 CHEVRON RD  RANGELY  CO 81648
Type Of Facility:UIC ENHANCED RECOVERYWell Status: AC
Facility NameRECTOR
Operator contact:DIANE  PETERSON
Location:  qtrqtr: SENE section: 16 township: 2N range: 103W meridian: 6
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:OTHER
Repair Desc:"well evaluation test" -- confirm integrity (well had failed 'routine' a few days prior)
Test Date:5/14/2007
Field Rep:
Approved Date:6/18/2007
Approved by:KRABACHER, JAY
Last Approved MIT:5/10/2006
Injection/Producing Formation Zones:WEBR
Perforation Interval:NA
Open Hole Interval:5586 - 6347
Bridge/Cement Plug Depth:
Tubing Size:2.875
Tubing Depth:6050
Top Packer Depth:5292
Multiple Packers:Y
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE810
5 MIN CASE810
CASE BEFORE0
FINAL CASE805
FINAL TUBE0
INITIAL TUBE0
LOSS OR GAIN-10
START CASE815
No channel test.