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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-26903TALLGRASS
16-17
KERR MCGEE OIL & GAS ONSHORE LP
47120
PA
12/13/2018
WATTENBERG
90750
ERIE/WELD  123
SESE 17 1N68W 6
335564
   
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Surface Casing Depth: 971 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
401642303Form 175/11/20185/16/2018 1WHISPER --0 DOWN TO 0 ----No----Surface casing produced no fluids. Surface casing shut in for 15 min ended with a whisper. Both tubing and production casing were LOTO.
400965223Form 1712/16/20151/6/2016 0DOWN TO 0 --0 DOWN TO 0 538543No----POST REMEDIATION TEST. SC DID NOT PRODUCE ANY FLUID. INITIAL POST REMEDIATION BLOWDOWN ON 12-8-15 STARTED WITH ZERO PSI AND BLEW DOWN TO ZERO.
400836046Form 174/20/20155/6/2015PLUNGER LIFT229GAS --121 WATER H20 866866No----SURFACE CASING PRODUCED 65 GALLONS OF WATER DURING TEST. MONITORED THE SURFACE CASING AN EXTRA 30 MINUTES, PRESSURE ENDED AT 94 PSI. SHUT THE SURFACE CASING IN FOR 15 MINUTES, PRESSURE BUILT BACK UP TO 154 PSI.
400766368Form 1711/17/20141/7/2015PLUNGER LIFT201GAS --121 WATER H20 573581No----SC PRODUCED 25 GALLONS OF WATER AND STOPPED TEST. SI SC FOR 15 MINS, ENDED WITH 165 PSI
400317526Form 178/8/20128/17/2012PLUNGER LIFT100GAS --<1 GAS 440456No----Surface casing produced no fluid during the form 17 test.