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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-005-07269POWELL
5-64 15-16-1CHZ
TRUE OIL LLC
90450
PR
8/1/2023
WILDCAT
99999
ARAPAHOE  005
NESE 15 5S64W 6
449920
   
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County Code: Sequence Code:
 
Surface Casing Depth: 2189 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
403994807Form 1710/23/202411/14/2024GAS LIFT0NO FLOW NONE0 NO FLOW 405445No---- 
403628231Form 1712/10/202312/18/2023 0NO FLOW --0 NO FLOW 345344No---- 
403279118Form 171/2/20231/4/2023PLUNGER LIFT0NO FLOW NONE0 NO FLOW 359355No---- 
402923771Form 171/6/20221/12/2022GAS LIFT0NO FLOW --0 NO FLOW 360350No---- 
402571724Form 171/6/20211/11/2021GAS LIFT0NO FLOW NONE0 NO FLOW 352357No---- 
402281527Form 171/5/20201/9/2020GAS LIFT0NO FLOW --0 NO FLOW 688716No---- 
401929938Form 172/4/20192/5/2019GAS LIFT0NO FLOW --0 NO FLOW 11091120No---- 
401854163Form 1711/28/201811/29/2018SHUT-IN300NO FLOW --0 NO FLOW 3030No----Bradenhead pressure was found to be 300 psig(most likely from thermal expansion). Pressure was bleed off and checked over 30 min and remained at zero. Have installed a pressure gauge and monitoring pressure. Tubing and packer are currently installed, tubing is shut in.
401520397Form 1711/16/20171/19/2018FLOWING0DOWN TO 0 --0 NO FLOW 11501150No----No flow observed during test. Test was performed during flowback operations.
401419367Form 1710/2/201710/3/2017SHUT-IN0NO FLOW --0 NO FLOW 30413002No----Test was performed to satisfy the COA for the Form 2. Performed during a stop in fracturing operations. The slight loss of pressure in the production casing can be attributed to formation leakoff. The bradenhead had zero pressure and zero flow.