403912931 | Form 17 | 9/7/2024 | 9/7/2024 | SHUT-IN | 0 | NO FLOW | NONE | 0 | NO FLOW | 462 | 462 | No | -- | -- | Annual 2024 bradenhead pressure test as required by COGCC rule. |
403343411 | Form 17 | 3/10/2023 | 3/10/2023 | SHUT-IN | 6 | DOWN TO 0 | VAPOR | 0 | NO FLOW | 440 | 440 | No | -- | -- | Annual 2023 bradenhead pressure test as required by COGCC rule. This bradenhead pressure test is also being used to close out a bradenhead mitigation plan in place for the well - Doc# 402653225 |
403021187 | Form 17 | 4/19/2022 | 4/19/2022 | SHUT-IN | 9 | DOWN TO 0 | WATER H20 | 0 | NO FLOW | 427 | 427 | No | -- | -- | Annual 2022 bradenhead pressure test as required by COGCC rule. |
402981199 | Form 17 | 3/1/2022 | 3/10/2022 | SHUT-IN | 8 | DOWN TO 0 | WATER AND GAS | 0 | NO FLOW | 425 | 425 | No | -- | -- | This test was performed to confirm bradenhead pressure mitigation work conducted in 10/2021. Pressure found on the bradenhead is within conforming parameters in COGCC guidance documents. This test is also being submitted as the 2022 annual bradenhead test as required per COGCC wellbore integrity rules. |
402864448 | Form 17 | 10/15/2021 | 11/9/2021 | SHUT-IN | 0 | NO FLOW | NONE | 0 | NO FLOW | 0 | 0 | No | -- | -- | Test was conducted after placement of an 80 barrel pill of 10 PPG mud down the bradenhead utilizing 1" tubing landed at 2250'. Immediately after placement of the heavy mud pill the fluid level in the bradenhead began to fall back. The bradenhead maintained full returns while placing the 10 PPG mud and only dirty water was circulated back.
It appears that the heavier mud provided enough additional hydrostatic pressure to shut off any water flowzone pressure.
Retrievable bridge plug from MIT was still present in the casing. Thus, no casing pressure was observed.
Another bradenhead test will be performed and reported prior to the end of the year. |
402566834 | Form 17 | 12/14/2020 | 1/5/2021 | SHUT-IN | 48 | DOWN TO 0 | WATER H20 | 1 | SURGE | 410 | 410 | No | -- | -- | 2020 bradenhead test performed on the Bradbury B#1 as required per adoption of COGCC rule to test all wells located in Adams County.
A water sample Analytical Sample Data Submittal Form 43 has been collected and submitted for the bradenhead fluid recovered from a 2019 bradenhead test performed 11/19/2019 and again after a prolonged bradenhead flow test concluded 9/15/2020. Both samples yielded very similar fluid analysis. Fluid recovered was approximately 7000 TDS.
A bradenhead remediation plan will now need to be submitted. In the interim the bradenhead will be flowed to the production tank to minimize the bradenhead back pressure exerted on non-cased formations. |
402318051 | Form 17 | 11/19/2019 | 2/26/2020 | SHUT-IN | 48 | WATER H20 | -- | 1 | WATER H20 | 395 | 395 | Yes | -- | Yes | Retest of the Bradbury B#1 to determine if bradenhead fluid pressure had built back from an earlier test performed 8/22/2019. A pressure of 48 psi was found and a fluid sample was obtained. Analysis of the fluid sample is attached and will also be submitted on an eForm 43.
A mitigation and remediation strategy will be discussed with COGCC staff. |
402148742 | Form 17 | 8/22/2019 | 2/20/2020 | SHUT-IN | 60 | WATER H20 | -- | 2 | WATER H20 | 380 | 380 | No | -- | -- | Initial bradenhead test performed on the Bradbury B#1 as required per adoption of COGCC new rule to test all wells located in Adams County. Well slugged water during the test. No clean water sampling containers were available at the time of the test. A future test and sample will be obtained. |