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Wellbore #00 Wellbore Classification: GW Status: SI - 6/1/2018 Measured TD: 6472 ft. Wellbore Data for Original Wellbore | Wellbore Classification: GW SI - 6/1/2018 | Wellbore Permit | | Permit #: | 19761352 | Expiration Date: | 12/30/1977 | Proposed Depth/Form: | 6500 ft. | Surface Mineral Owner Same: | Not available | Mineral Owner: | STATE | Surface Owner: | Not available | Unit: | | Unit Number: | | Formation And Spacing: | Code: JSND , Formation: J SAND , Order: 0 , Unit Acreage: 40, Drill Unit: SWNW |
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Wellbore Completed | Completion Date: | 2/12/1977 | Spud Date: | 1/15/1977 | Spud Date Is: | ACTUAL | Measured TD: | 6472 ft. | Measured PB depth: | 6438 ft. | True Vertical TD: | | True Vertical PB depth: | | Log Types: | IES, CDL-FDC-GR | Casing: | String Type: SURF, Hole Size: 12.25 in., Size: 8.625 in., Top: 0 ft., Depth: 202 ft., Weight: 24 , Citings Type: ACTUAL | Cement: | Sacks: 160, Top: 0 ft., Bottom: , Determination Method: | Casing: | String Type: 1ST, Hole Size: 7.875 in., Size: 4.5 in., Top: 0 ft., Depth: 6572 ft., Weight: 10.5 , Citings Type: ACTUAL | Cement: | Sacks: 150, Top: 0 ft., Bottom: , Determination Method: | Formation | Interval Top | Log Bottom | Cored | DSTs | NIOBRARA | 5473 ft. | | | | FORT HAYS | 5820 ft. | | | | CARLILE | 5867 ft. | | | | GREENHORN | 5930 ft. | | | | BENTONITE | 6154 ft. | | | | D SAND | 6251 ft. | | | | J SAND | 6324 ft. | | | | SKULL CREEK | 6463 ft. | | | |
Formation JSND Formation Classification: GW Status: SI - 6/1/2018 Interval Top: 6356 ft. Interval Bottom: 6372 ft. Completed Information for Formation J SAND | 1st Production Date: | 3/14/1977 | Choke Size: | 0.750 in. | Formation Name: | J SAND | Commingled: | | Production Method: | FLOWING | Open Hole Completion: | |
| Formation Treatment | Treatment Date: | 2/12/1977 | Treatment Summary: | SEE DOCUMENT # 368366 |
| Tubing Size: | 1.9 in. | Tubing Setting Depth: | 6330 ft. | Tubing Packer Depth: | | Tubing Multiple Packer: | | Open Hole Top: | | Open Hole Bottom: | | Initial Test Data: | Test Date: | 2/14/1977 | Test Method: | FLOWING | Hours Tested: | 24 | Gas Type: | | Gas Disposal: | VENTED | |
Test Type | Measure |
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CALC_MCF_GAS | 330 | CASING_PRESS | 140 | MCF_GAS | 330 | TUBING_PRESS | 15 |
| Perforation Data: | Interval Top: | 6356 ft. | # Of Holes: | | Interval Bottom: | 6372 ft. | Hole Size: | |
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Reported Plugged | N | |
Out Of Service Repurposed | N | |
Out Of Service | N | |
Inactive Exception | N | |
Noticed Inactive | N | |
Defined Inactive (SI ) | Y | Defined Inactive 05/31/2018 |
Low Producing | Y | Production Period 02/2024 - 01/2025 |
Total Oil Produced (Barrels) | 0 |
Total Gas Produced (MCF) | 0 |
GOR | |
GOR Determination | MCFE |
Average BOE per Day | 0.000 |
Average MCFE per Day | 0.000 |
Federal Financial Assurance | i | |
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