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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-39075Becker Ranch
5E-403
PDC ENERGY INC
69175
PR
12/6/2015
WATTENBERG
90750
WELD  123
NWNW 5 3N64W 6
436361
   
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Surface Casing Depth: 925 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
404182082Form 174/14/20254/28/2025PLUNGER LIFT3DOWN TO 0 GAS0 NO FLOW 217218No----Remediation follow up test. 3 PSI blew down to 0 PSI within first few seconds of test. No pressure or flow observed for the remainder of the test. Operator will monitor pressure and re-test according to bradenhead policy.
403773380Form 174/22/20244/30/2024PLUNGER LIFT54DOWN TO 0 GASTSTM WHISPER 208222No----Annual test. 54 PSI blew down to almost 0 in seconds, whisper gas for entire test. PDC will monitor pressure and re-test according to bradenhead policy.
403480892Form 177/28/20237/31/2023PLUNGER LIFT67CONTINUOUS GAS0 NO FLOW 296302Yes----High Pressure Verification test. 67 PSI gas flow blew down to 0 PSI in 5 minutes. PDC will schedule a sampling event and submit results via form 43. PDC will monitor pressure and re-test according to bradenhead policy.
Click for SpecificsFull4/5/20234/10/2023 0Down to Zero--0Down to Zero383382NoNoneNoneAnnual Test. 0 PSI, with no pressure or flow observed for the entire 30-minute test. PDC will continue to monitor monthly.
Click for SpecificsFull6/15/20227/6/2022 2Down to Zero--0Down to Zero164168NoNoneNone 
Click for SpecificsFull8/1/202111/1/2021 0Down to Zero--0No Flow195198NoNoneNone 
Click for SpecificsLight8/31/202012/3/2020 10 --0No Flow289289NoNoNo 
Click for SpecificsLight7/13/20198/18/2020 0 --0 347347NoNoNo