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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-31135SHERWOOD L FEDERAL
30-29D
KERR MCGEE OIL & GAS ONSHORE LP
47120
PA
8/29/2023
WATTENBERG
90750
PLATTEVILLE/WELD  123
NWNW 30 3N66W 6
336438
   
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Surface Casing Depth: 607 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
403175798Form 179/22/20229/22/2022 244CONTINUOUS GAS3 CONTINUOUS 732732No----Tubing Shut in. Surface Casing produced Water.
403118850Form 177/27/20227/27/2022 131CONTINUOUS GAS1 WHISPER 649652YesYesYesSurface Casing produced Water.
402904371Form 1712/17/202112/20/2021 3CONTINUOUS GAS1 WHISPER 671673No----Surface Casing produced no liquid.
402537060Form 1710/2/202011/20/2020 253CONTINUOUS WATER H208 CONTINUOUS 321321No----Surface Casing produced Water.
Click for SpecificsFull7/3/201912/10/2019 250Gas 1Whisper (Very Low Flow)255275YesYesYesSurface casing produced water.
400835441Form 174/20/20155/5/2015PLUNGER LIFT242GAS --1 GAS 518522No----SURFACE CASING PRODUCED 18 GALLONS OF WATER DURING FORM 17 TEST. MONITORED THE SURFACE CASING AN EXTRA 30 MINUTES, PRESSURE STAYED AT A WHISPER. SHUT THE SURFACE CASING IN FOR 15 MINUTES, PRESSURE STAYED AT A WHISPER. POST REMEDIATION BLOW-DOWN ON 4-10-2015, PRESSURE AT 252 PSI AND BLEW-DOWN TO 1 PSI.
400985547Form 173/26/20142/8/2016 162GAS --19 GAS ----No----SC PRODUCED 3 GALLONS OF WATER. WELL WAS SHUT IN AND TORN APART. CASING INACCESSIBLE. BLEW DOWN AN ADDITIONAL 30 MIN. WELL PRESSURED UP TO #50 AFTER 30 MIN WHILE PRODUCING WATER.