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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-30716CAMP
41-24
KERR MCGEE OIL & GAS ONSHORE LP
47120
PR
10/1/2023
WATTENBERG
90750
WELD  123
SENE 24 3N67W 6
336160
   
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Surface Casing Depth: 877 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
Click for SpecificsFull10/30/202511/11/2025 2ContinuousNone0No Flow906906NoNN Surface Casing produced no liquid.
Click for SpecificsFull6/4/202410/28/2024 2ContinuousNone--No Flow871874NoNN Tubing Shut in. Surface Casing produced no liquid.
Click for SpecificsFull6/5/20237/17/2023Plunger Lift3ContinuousNone--No Flow850851NoNN Tubing Shut in. Surface Casing produced no liquid.
Click for SpecificsFull6/27/20227/11/2022Plunger Lift1WhisperNone--No Flow886884NoNN Surface Casing produced no liquid.
Click for SpecificsFull8/30/20219/13/2021Plunger Lift5ContinuousNone--No Flow739741NoNN Surface Casing produced no liquid.
Click for SpecificsFull6/4/202011/2/2020 32Continuous Flow 0Down To Zero15591559NoNoNo Surface Casing produced no liquid.
401921506Form 171/23/20191/29/2019 40GAS --0 DOWN TO 0 574444No----SURFACE CASING PRODUCED NO FLUIDS. SHUT-IN FOR 15 MIN; ENDED WITH 0 PSI.
401066704Form 176/14/20166/22/2016 1GAS --0 DOWN TO 0 687687No----POST REMEDIATION TEST. SC DID NOT PRODUCE ANY FLUID. 15 MIN BUILD UP, DEAD. DEMCO CLOSED AND WELL SHUT IN UPON ARRIVAL. INITIAL POST REMEDIATION BLOWDOWN ON 6-8-16 STARTED WITH 80 PSI AND BLEW DOWN TO ZERO PSI.
400353537Form 1710/25/201212/4/2012PLUNGER LIFT73GAS --0 DOWN TO 0 343365No----No fluid was produced during form 17 test.