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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-25139ST. ACACIUS
29-35
KERR MCGEE OIL & GAS ONSHORE LP
47120
PA
7/18/2019
WATTENBERG
90750
MEAD/WELD  123
SWNW 35 3N68W 6
336490
   
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Surface Casing Depth: 895 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
402043239Form 174/30/20195/14/2019PLUNGER LIFT23GAS --1 WATER H20 583585Yes----Surface casing produced water. Well shut in for 15min ended with psi. Surface casing blown down an extra 30min ended with a whisper.
400835437Form 174/17/20155/5/2015PLUNGER LIFT20GAS --0 DOWN TO 0 20592059No----POST REMEDIATION TEST. INITIAL POST REMEDIATION BLOW-DOWN ON 4-9-2015 STARTED WITH 18 PSI, BLEW-DOWN TO 0 PSI. SURFACE CASING DID NOT PRODUCE ANY FLUID. 15 MINUTE BUILD-UP, WHISPER. OPEN TO SALES, TEMP. SHUT-IN FOR HZ PREP, AND TORN APART UPON ARRIVAL.
400803161Form 172/13/20153/4/2015PLUNGER LIFT26GAS --0 DOWN TO 0 16181618No----SURFACE CASING DID NOT PRODUCE ANY FLUID. WELL WAS TEMPORARILY SHUT-IN FOR HZ PREP., AND TORN APART UPON ARRIVAL. 15 MINUTE BUILD-UP, WHISPER.
400290218Form 174/19/20125/29/2012PLUNGER LIFT348GAS --152 GAS 373377No----No fluid was produced during 30 minute blow down