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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-21701DAVIS
12-15
KERR MCGEE OIL & GAS ONSHORE LP
47120
PA
3/8/2024
WATTENBERG
90750
WELD  123
NWSW 15 3N67W 6
332005
   
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Surface Casing Depth: 722 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
Click for SpecificsFull1/5/20242/12/2024Plunger Lift0No FlowNone--No Flow00NoNN Tubing Shut in. Surface Casing produced no liquid.
403610804Form 1711/30/202311/30/2023 24CONTINUOUS GAS0 NO FLOW 831827YesYesNoTubing Shut in. Surface Casing produced no liquid.
403233264Form 1711/16/202211/17/2022 20CONTINUOUS GAS1 WHISPER 856861No----Tubing Shut in. Surface Casing produced no liquid.
402647127Form 174/1/20214/2/2021 25CONTINUOUS GAS0 NO FLOW 885885No----Tubing Shut in. Surface Casing produced no liquid.
402602742Form 172/10/20212/18/2021 297CONTINUOUS GAS4 CONTINUOUS 894894No----Tubing Shut in. Surface Casing produced no liquid.
402601987Form 172/10/20212/17/2021 297CONTINUOUS GAS4 CONTINUOUS 894894No---- Tubing Shut in. Surface Casing produced no liquid.
402505142Form 1710/5/202010/7/2020 26CONTINUOUS --0 NO FLOW 893893No----Tubing Shut in. Surface Casing produced no liquid.
Click for SpecificsFull12/14/201912/20/2019 286Gas--1Gas863862NoNoNoTubing shut in. Surface casing produced no liquids.
400417895Form 175/6/20135/14/2013PLUNGER LIFT154GAS --118 WATER H20 528535No----Surface casing made 50 gallons of muddy water in first 15 minutes of test. Surface casing was shut in and tank emptied. Test resumed for final 15 minutes. Surface casing made 100 gallons of muddy water during 30 minute blow down.