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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-057-06508Coalmont
3-13H
FULCRUM ENERGY OPERATING LLC
10805
TA
2/4/2026
NORTH PARK HORIZONTAL NIOBRARA
60120
JACKSON  057
SWSW 13 7N81W 6
421227
   
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Surface Casing Depth: 1011 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
404547719Form 172/12/20262/18/2026SHUT-IN80CONTINUOUS WATER H200 CONTINUOUS 00Yes--YesProduction casing inaccessible for sample. BHD produced about 60 gallons of fluid during the test. MIT was recently completed and the fluid appears to be similar with the pressure test fluids. Samples were taken and will confirm.
404343395Form 177/1/20259/5/2025SHUT-IN80WHISPER GAS0 NO FLOW 50--YesYes--Initial gas, but slowed down to a whisper and stayed at low pressure for ~15 min, then died and stayed dead. Test was completed on 7/1/25 on paper Form 17 in the field. The paper copy was stuck between pages in the scan and wasn't noticed missing until now.
403881149Form 177/22/20248/7/2024SHUT-IN45DOWN TO 0 GAS0 NO FLOW 150--YesYes-- 
Click for SpecificsFull7/18/20239/25/2023Pumping50Whisper----No Flow5050NoNoNo 
403270494Form 1712/20/202212/22/2022PUMPING2DOWN TO 0 GAS0 NO FLOW 2929YesYes-- 
402953389Form 172/8/20222/10/2022SHUT-IN33DOWN TO 0 NONE0 NO FLOW 8989No----Flameless heater placed on bradenhead valve for ~10 minutes prior to test.