Formation Treatment |
Treatment Type: | ACID JOB |
Treatment Date: | 2/11/2021 | Treatment End Date: | 2/11/2021 |
Treatment Summary: | PUMPED 2000 GALLONS (47.6 BBLS) 15% HCL W/6% CITRIC ACID WITH MUTUAL SOLVENT AND 47 BBLS WATER |
Total fluid used in treatment (bbls): | 96 | Max pressure during treatment (psi): | 2300 |
Total gas used in treatment (mcf): | | Fluid density (lbs/gal): | |
Type Of gas: | | Number Of staged intervals: | |
Total acid used in treatment (bbls): | 47 | Min frac gradient (psi/ft): | |
Recycled water used in treatment (bbls): | | Total flowback volume recovered (bbls): | |
Fresh water used in treatment (bbls): | 47 | Disposition method For flowback: | |
Total proppant used (lbs): | | Green completions techniques utilized: | -- |
Reason green techniques Not utilized: |
Formation Treatment |
Treatment Type: | ACID JOB |
Treatment Date: | 2/20/2019 | Treatment End Date: | 2/20/2019 |
Treatment Summary: | INJECTION WELL SHUT IN ON 5/31/2018 FOR HIGH CASING PRESSURE. FISH PACKERS AND SELECTIVE INJECTION EQUIPMENT. 2 CASING CEMENT SQUEEZE JOBS (REPORTED ON FORM 5 #401950505. RAN 5 1/2" CASING FROM SURFACE TO 6181'.
RAN 195 JTS NEW FIBERLINED TUBING ANDF PACKERS. WITNESSED MIT SCHEDULED FOR MARCH 6TH, WELL TO BE RETURNED TO INJECTION UPON APPROVAL. |
Total fluid used in treatment (bbls): | 128 | Max pressure during treatment (psi): | 1125 |
Total gas used in treatment (mcf): | | Fluid density (lbs/gal): | |
Type Of gas: | | Number Of staged intervals: | |
Total acid used in treatment (bbls): | 48 | Min frac gradient (psi/ft): | |
Recycled water used in treatment (bbls): | | Total flowback volume recovered (bbls): | |
Fresh water used in treatment (bbls): | 80 | Disposition method For flowback: | |
Total proppant used (lbs): | | Green completions techniques utilized: | -- |
Reason green techniques Not utilized: |
Formation Treatment |
Treatment Type: | ACID JOB |
Treatment Date: | 6/29/2015 | Treatment End Date: | 6/29/2015 |
Treatment Summary: | Pumped 4000 gallons 15% Hcl w/ 330 gallons of solvent at 3.5 bpm @ 2100 psi |
Total fluid used in treatment (bbls): | 192 | Max pressure during treatment (psi): | |
Total gas used in treatment (mcf): | | Fluid density (lbs/gal): | |
Type Of gas: | | Number Of staged intervals: | |
Total acid used in treatment (bbls): | 95 | Min frac gradient (psi/ft): | |
Recycled water used in treatment (bbls): | | Total flowback volume recovered (bbls): | |
Fresh water used in treatment (bbls): | 89 | Disposition method For flowback: | |
Total proppant used (lbs): | | Green completions techniques utilized: | -- |
Reason green techniques Not utilized: |
Formation Treatment |
Treatment Date: | 9/15/2010 |
Treatment Summary: | ACID STIMULATION 9/15/10 PUMPED 4000 GALLONS OF 20% HCI THROUGH END OF COLIED TUBING 6220' AT STARTING PRESSURE OF 1700 PSI. |
Formation Treatment |
Treatment Date: | 10/13/2009 |
Treatment Summary: | ACID STIMULATION 10/13/09 PUMPED 4000 GALLONS OF 20% HCI THROUGH TUBING. |