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COGIS DB

 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-10877PICEANCE CREEK UNIT
297-13A9
QB ENERGY OPERATING LLC
10844
PR
9/1/2025
PICEANCE CREEK
68800
RIO BLANCO  103
SWNE 13 2S97W 6
336011View Related
 
COGIS - Conditions of Approval Results
TypeSource DocumentConditions of Approval
EngineerForm: (04)
404465024
02/04/2026
Well to be plugged or repaired within 6 months of identifying the integrity issue . Pressure is to be managed and mitigated until plugging or repair is complete.
EngineerForm: (04)
404465024
02/04/2026
1. Operator will implement measures to control venting, to protect health and safety, and to ensure that vapors and odors from well operations do not constitute a nuisance or hazard to public welfare. 2. Shut in bradenhead pressure shall not exceed threshold pressure. 3. If a sample has not been collected within the last twenty four months collect intermediate and production gas samples for laboratory analysis. Sampling will comply with Operator Guidance - Bradenhead Testing and Reporting Instructions, Appendix A: Liquid and Gas Sampling. Copies of all final laboratory analytical results will be provided to the COGCC within three months of collecting the samples. 4. For applicable operations, report work completed within 30 days on a Form 4 Sundry REPORT OF WORK DONE - Repair Well noting final pressure test results and include any operational or job summaries. If the wellbore geometry changes or there is not an updated WBD in the well file submit an updated WBD. 5. Complete a bradenhead test within 30 days of completing the repair and submit results on a Form 17
EngineerForm: (04)
404608485
04/30/2026
DOC 404500259 Form 17 6/18/2025 - Production pressure reduces during intermediate test DOC 404500259 Form 17 1/8/2026 - post wellhead repair - Production pressure reduces during intermediate test Well has exceeded 6 month repair or plug timeline Operators comments and plans:Production pressure fell during the INT test. After the initial test, QB repacked the wellhead. A second BH test was conducted to determine results of wellhead work. Based on the results, QB proposes to P&A the wellbore.
 
COGIS - Best Management Practice Results
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