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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-07537CARNEY C T
29 X 34
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
1/1/2024
RANGELY
72370
RIO BLANCO  103
NWSE 34 2N102W 6
314912View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:12/1/1998MIT Assigned By:ADKINS, JAIME
Date Recv'd:4/22/2003Facility ID: 150200
DocNum:623001Facility Status:AC
Operator Information:
Oper. No.16700
Operator:CHEVRON U S A INC
Address:P O BOX 4791  HOUSTON  TX 77210-4791
Type Of Facility:UIC ENHANCED RECOVERYWell Status: AC
Facility NameCARNEY C T
Operator contact: 
Location:  qtrqtr: SENE section: 16 township: 2N range: 103W meridian: 6
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:TUBING/PACKER LEAK
Repair Desc:PULLED PRODUCTION EQIPMENT INSTALLED INJECTION EQUIPMENT TO CONVERT TO INJECTION
Test Date:10/1/1998
Field Rep:
Approved Date:4/22/2003
Approved by:ADKINS, JAIME
Last Approved MIT:N/A
Injection/Producing Formation Zones:WEBR
Perforation Interval:5631-6334
Open Hole Interval:NA
Bridge/Cement Plug Depth:NA
Tubing Size:2.875
Tubing Depth:6258
Top Packer Depth:5400
Multiple Packers:N
 
Condition of approval:
INITIAL TEST
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE775
5 MIN CASE765
CASE BEFORE
FINAL CASE800
FINAL TUBE0
INITIAL TUBE0
LOSS OR GAIN-45
START CASE755
No channel test.