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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-08494FEE
119X
SCOUT ENERGY MANAGEMENT LLC
10779
PA
8/16/2007
RANGELY
72370
RIO BLANCO  103
NENE 29 2N102W 6
397970View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:2/2/1999MIT Assigned By:ADKINS, JAIME
Date Recv'd:4/15/2003Facility ID: 150200
DocNum:621771Facility Status:AC
Operator Information:
Oper. No.16700
Operator:CHEVRON U S A INC
Address:P O BOX 4791  HOUSTON  TX 77210-4791
Type Of Facility:UIC ENHANCED RECOVERYWell Status: AC
Facility NameFEE
Operator contact: 
Location:  qtrqtr: SENE section: 16 township: 2N range: 103W meridian: 6
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:TUBING/PACKER AND CASING LEAK
Repair Desc:
Test Date:1/26/1999
Field Rep:
Approved Date:3/18/1999
Approved by:ADKINS, JAIME
Last Approved MIT:12/2/1997
Injection/Producing Formation Zones:WEBR
Perforation Interval:5792-6427
Open Hole Interval:
Bridge/Cement Plug Depth:NA
Tubing Size:2.875
Tubing Depth:6357
Top Packer Depth:5596
Multiple Packers:Y
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE720
5 MIN CASE760
CASE BEFORE
FINAL CASE710
FINAL TUBE0
INITIAL TUBE0
LOSS OR GAIN60
START CASE770
No channel test.