Form 21 | Related Doc |
Date Submitted: | 1/17/2024 | MIT Assigned By: | |
Date Recv'd: | 1/17/2024 | Facility ID: | |
DocNum: | 403657580 | Facility Status: | |
Operator Information: |
Oper. No. | 10779 |
Operator: | SCOUT ENERGY MANAGEMENT LLC |
Address: | 13800 MONTFORT DRIVE SUITE 100 DALLAS TX 75240 |
Type Of Facility: | | Well Status: |
Facility Name | CARNEY C T |
Operator contact: | Anita Sanford |
Location: | | qtrqtr: | section: | township: | range: | meridian: |
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MIT Details: |
Test Type: | VERIFICATION OF REPAIRS |
Repair Type: | |
Repair Desc: | Casing leak found from 3526'-3801'. TOC was at 3850'. Made decision to circulate cement through leak all the way to surface. Pumped 370 sks 13.4#/1.61 yield premium G cmt and got returns to surface. Clean out cement and CICR and chart test casing to 1250 psi - Passed rig test. RIH w/ injection equipment. Return to injection pending an approved Form 21. |
Test Date: | 1/15/2024 |
Field Rep: | Browning, Chuck |
Approved Date: | 1/17/2024 |
Approved by: | |
Last Approved MIT: | 9/26/2018 |
Injection/Producing Formation Zones: | WEBR |
Perforation Interval: | 5630-6338 |
Open Hole Interval: | |
Bridge/Cement Plug Depth: | |
Tubing Size: | 2.875 |
Tubing Depth: | 5977 |
Top Packer Depth: | 5345 |
Multiple Packers: | |
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Condition of approval: |
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Test Data: | Wellbore Channel Test: | Reading Type | Pressure | 10 MIN CASE | 1350 | 5 MIN CASE | 1355 | FINAL CASE | 1350 | LOSS OR GAIN | -10 | START CASE | 1360 |
| No channel test. |
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