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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-05809MCLAUGHLIN, A C
7
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
8/17/2023
RANGELY
72370
RIO BLANCO  103
SWNE 14 2N103W 6
314483View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:5/25/2023MIT Assigned By:
Date Recv'd:5/25/2023Facility ID: 
DocNum:403413341Facility Status:
Operator Information:
Oper. No.10779
Operator:SCOUT ENERGY MANAGEMENT LLC
Address:13800 MONTFORT DRIVE SUITE 100  DALLAS  TX 75240
Type Of Facility:Well Status: 
Facility NameMCLAUGHLIN, A C
Operator contact:Anita  Sanford
Location:  qtrqtr:  section:  township:  range:  meridian: 
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:
Repair Desc:UIC REPAIR ADDED WEBER ZONE 1 & 3 PERFORATIONS FROM 6582-6639 AND 6396-6468 @ 3 SPF 120 PHASING WITH 21 GRAM 44" SHOT PEN. ACIDIZE. Return to injection pending an approved Form 21.
Test Date:5/24/2023
Field Rep:Browning, Chuck
Approved Date:5/25/2023
Approved by:
Last Approved MIT:7/19/2018
Injection/Producing Formation Zones:WEBR
Perforation Interval:6396-6639
Open Hole Interval:
Bridge/Cement Plug Depth:
Tubing Size:2.875
Tubing Depth:6396
Top Packer Depth:6306
Multiple Packers:
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE1290
5 MIN CASE1290
FINAL CASE1290
FINAL TUBE1573
INITIAL TUBE1573
LOSS OR GAIN-10
START CASE1300
No channel test.