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COGIS - Remediation Reports
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-123-23256PSC
2-10
KERR MCGEE OIL & GAS ONSHORE LP
47120
PA
4/13/2023
WATTENBERG
90750
WELD  123
NENE 10 3N67W 6
332536View Related Related
 
Form 27/27AView Related Related View DocsDoc
Date Submitted:3/6/2023
Date Recv'd:3/6/2023Assigned by:Taylor Robinson
DocNum:403322330API number:05-123-23256
Document Type:FORM 27 Project Number:28172
Operator Information:
Operator:KERR MCGEE OIL & GAS ONSHORE LP
Oper. No.47120
Address:P O BOX 173779  DENVER  CO 80217-3779
Type Of Facility:SPILL OR RELEASE
Fac. NamePSC 2-10 WH Workover Release
County Name:WELD
Operator contact:Gregory Hamilton
qtrqtr: NENEsection: 10township: 3Nrange: 67Wmeridian: 6
Remediation Details:
Impacted Media
MediaImpactedExtentHow Determined?
GROUNDWATER UTBD Groundwater samples/laboratory analytical results
SOILS UTBD Inspection/soil samples/laboratory analytical results
Reason for Report: OTHER
Cause of Condition: OTHER
Potential Receptors: Multiple buildings and livestock holding pens are located within ΒΌ mile of the wellhead. A building
 
HOW REMEDIATE:  Potential impacts that meet the criteria in Rule 912.b. will be reported to the Director in accordance with that Rule and a site-specific soil and/or groundwater remediation plan will be developed and submitted to the COGCC via a supplemental Form 27 in accordance with Rule 913. If reportable impacts are not encountered, a supplemental Form 27 requesting closure will be submitted within 90 days following completion of sampling activities. Field screening and applicable laboratory analytical results will be reported in all submittals. E&P waste records of material transported off-site are kept on file and available upon request.
 
INITIAL ACTION:  This form has been prepared to provide prior notice of the plugging and abandonment of the PSC 2-10 wellhead and the removal of the flowlines associated with wellheads PSC 2-10 and PSC-10A. The PSC-1-10A wellhead was plugged and abandoned and the flowline status was changed to Out-of-Service on October 19, 2021. The flowlines will be permanently removed. The off-location flowline system pre-removal notices were submitted under Form 44 Document Nos. 403314613 and 403333997. In accordance with COGCC Rule 911.a., soil and groundwater (if present) samples will be collected and submitted for laboratory analysis to determine if concentrations and values are in compliance with COGCC Table 915-1. Visual inspection and field screening of soils around the PSC 2-10 wellhead and associated flowlines will be conducted during sampling activities. Soil vapor screening will also be performed around the PSC 2-10 wellhead. The topographic Site Location Map showing the geographic setting of the site is provided as Figure 1.
 
RECLAMATION PLAN:  The site will be reclaimed in accordance with COGCC 1000 Series Reclamation Rules.
 
SOURCE REMOVED:  If a suspected release is identified and confirmed through soil screening and/or laboratory analysis, soils will be removed and transported to a licensed disposal facility. Disposal records will be kept on file and available upon request.
 
Correspondence Log:
Final Resolution
DateCase Closed?Letter Sent?CECMC Person
8/10/2023YTaylor Robinson
N/ANTaylor Robinson
 
Coordinates:
TypeFacility IDFacility Name/NumLat/Long
Remediation250516HSR-PSC
1-10A
40.245980/-104.870110

Facility280254PSC
2-10
40.245780/-104.870170

Remediation484434PSC 2-10 WH Workover Release
40.245790/-104.870218