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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-07594FEE
94X
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
6/1/2020
RANGELY
72370
RIO BLANCO  103
SENE 33 2N102W 6
314944View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:6/11/2015MIT Assigned By:
Date Recv'd:6/11/2015Facility ID: 
DocNum:400852368Facility Status:
Operator Information:
Oper. No.16700
Operator:CHEVRON PRODUCTION COMPANY
Address:100 CHEVRON RD  RANGELY  CO 81648
Type Of Facility:Well Status: 
Facility NameFEE
Operator contact:DIANE  PETERSON
Location:  qtrqtr:  section:  township:  range:  meridian: 
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:
Repair Desc:CLEAN OUT WELLBORE, ACIDIZE PERFS, RIH WITH NEW TBG & PKR. PACKER DEPTH APPROVAL DOC#400844322
Test Date:6/10/2015
Field Rep:Browning, Chuck
Approved Date:8/7/2015
Approved by:
Last Approved MIT:7/30/2012
Injection/Producing Formation Zones:WEBR
Perforation Interval:5584-6332
Open Hole Interval:
Bridge/Cement Plug Depth:
Tubing Size:2.875
Tubing Depth:6358.5
Top Packer Depth:5391.6
Multiple Packers:
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE1300
5 MIN CASE1300
FINAL CASE1300
START CASE1300
No channel test.