Skip to Main Content

Incident Search

COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-06426MCLAUGHLIN A C
54X
SCOUT ENERGY MANAGEMENT LLC
10779
PR
8/25/1994
RANGELY
72370
RIO BLANCO  103
NESW 23 2N103W 6
314699View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:4/9/2002MIT Assigned By:ADKINS, JAIME
Date Recv'd:4/25/2003API number: 05-103-06426
DocNum:200037907Facility Status:PR
Operator Information:
Oper. No.16700
Operator:CHEVRON U S A INC
Address:P O BOX 4791  HOUSTON  TX 77210-4791
Type Of Facility:WELLWell Status: PR
Well Name/No.MCLAUGHLIN A C
Operator contact: 
Location:  qtrqtr: NESW section: 23 township: 2N range: 103W meridian: 6
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:CASING LEAK
Repair Desc:C/O 7 INCH CSG TO 5 INCH LINER TOP. TEST CSG. RAN SUR-LOC PKR ON FIBERLINE TBG
Test Date:1/22/2002
Field Rep:
Approved Date:4/3/2003
Approved by:ADKINS, JAIME
Last Approved MIT:11/13/1995
Injection/Producing Formation Zones:WEBR
Perforation Interval:6132-6606
Open Hole Interval:NA
Bridge/Cement Plug Depth:NA
Tubing Size:2.875
Tubing Depth:5717
Top Packer Depth:5680
Multiple Packers:N
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE900
5 MIN CASE890
CASE BEFORE
FINAL CASE910
FINAL TUBE
INITIAL TUBE
LOSS OR GAIN20
START CASE890
No channel test.