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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-07581FEE
85X
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
1/1/2024
RANGELY
72370
RIO BLANCO  103
SESE 29 2N102W 6
314936View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:1/21/2013MIT Assigned By:ONYSKIW, DENISE
Date Recv'd:1/24/2013Facility ID: 150200
DocNum:1772338Facility Status:AC
Operator Information:
Oper. No.16700
Operator:CHEVRON USA INC
Address:6001 BOLLINGER CANYON RD  SAN RAMON  CA 94583
Type Of Facility:UIC ENHANCED RECOVERYWell Status: AC
Facility NameFEE
Operator contact:DIANE L.  PETERSON
Location:  qtrqtr: SENE section: 16 township: 2N range: 103W meridian: 6
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:TUBING/PACKER LEAK
Repair Desc:RUN 5-1/2" LINER FROM SURFACE TO 6330' - RE-PERF 5566-6329' RUN 171 JOINTS 2-7/8" FIBERLINED TBG.
Test Date:1/17/2013
Field Rep:
Approved Date:2/8/2013
Approved by:ONYSKIW, DENISE
Last Approved MIT:5/15/2008
Injection/Producing Formation Zones:WEBR
Perforation Interval:5566-6329
Open Hole Interval:NA
Bridge/Cement Plug Depth:NA
Tubing Size:2.875
Tubing Depth:5586
Top Packer Depth:5500
Multiple Packers:Y
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE
5 MIN CASE
CASE BEFORE
FINAL CASE1200
FINAL TUBE
INITIAL TUBE
LOSS OR GAIN0
START CASE1200
No channel test.