Form 21 | Related Doc |
Date Submitted: | 9/27/2012 | MIT Assigned By: | KOEHLER, BOB |
Date Recv'd: | 10/1/2012 | Facility ID: | 150200 |
DocNum: | 1772042 | Facility Status: | AC |
Operator Information: |
Oper. No. | 16700 |
Operator: | CHEVRON USA INC |
Address: | 6001 BOLLINGER CANYON RD SAN RAMON CA 94583 |
Type Of Facility: | UIC ENHANCED RECOVERY | Well Status: AC |
Facility Name | CARNEY C T |
Operator contact: | DIANE L. PETERSON |
Location: | | qtrqtr: SENE | section: 16 | township: 2N | range: 103W | meridian: 6 |
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MIT Details: |
Test Type: | VERIFICATION OF REPAIRS |
Repair Type: | OTHER |
Repair Desc: | Liner: Run 5-1/2" 17# liner surface to 5409'. |
Test Date: | 9/26/2012 |
Field Rep: | |
Approved Date: | 10/2/2012 |
Approved by: | KOEHLER, BOB |
Last Approved MIT: | 5/14/2008 |
Injection/Producing Formation Zones: | WEBR |
Perforation Interval: | 5692-6488 |
Open Hole Interval: | NA |
Bridge/Cement Plug Depth: | NA |
Tubing Size: | 2.875 |
Tubing Depth: | 5464 |
Top Packer Depth: | 5373 |
Multiple Packers: | Y |
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Condition of approval: |
Top of 1st 5" liner (January 1986) is 5409' so Top Packer depth acceptable. Bottom of perfs probably inaccurate; CICR set at 6288' (1st string) and 6290' (1st liner) at 2 different times and squeezed. Also 100 sx squeeze of 1st liner; 6238'-6243'. |
Test Data: | Wellbore Channel Test: | Reading Type | Pressure | 10 MIN CASE | | 5 MIN CASE | | CASE BEFORE | | FINAL CASE | 1750 | FINAL TUBE | | INITIAL TUBE | | LOSS OR GAIN | 0 | START CASE | 1750 |
| No channel test. |
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