Form 21 | Related Doc |
Date Submitted: | 4/15/2011 | MIT Assigned By: | KOEHLER, BOB |
Date Recv'd: | 4/18/2011 | API number: | 05-103-07110 |
DocNum: | 1771298 | Facility Status: | PR |
Operator Information: |
Oper. No. | 16700 |
Operator: | CHEVRON USA INC |
Address: | 100 CHEVRON ROAD RANGELY CO 81648 |
Type Of Facility: | WELL | Well Status: PR |
Well Name/No. | M B LARSON |
Operator contact: | DIANE L. PETERSON |
Location: | | qtrqtr: SENE | section: 26 | township: 2N | range: 102W | meridian: 6 |
|
MIT Details: |
Test Type: | VERIFICATION OF REPAIRS |
Repair Type: | CASING LEAK |
Repair Desc: | FEDERAL LEASE-Fed M.B. Larson D D-052241 SHUT-IN WELL-TESTED FOR TA STATUS, FAILED-REPAIRED CASING LEAK-CEMENT SQUEEZE-RETURNED WELL TO ACTIVE PRODUCTION. |
Test Date: | 3/25/2011 |
Field Rep: | |
Approved Date: | 4/18/2011 |
Approved by: | KOEHLER, BOB |
Last Approved MIT: | N/A |
Injection/Producing Formation Zones: | WEBR |
Perforation Interval: | 6121-6490 |
Open Hole Interval: | NA |
Bridge/Cement Plug Depth: | NA |
Tubing Size: | 2.875 |
Tubing Depth: | 6003 |
Top Packer Depth: | 5936 |
Multiple Packers: | N |
|
Condition of approval: |
|
Test Data: | Wellbore Channel Test: | Reading Type | Pressure | 10 MIN CASE | 750 | 5 MIN CASE | 750 | CASE BEFORE | | FINAL CASE | 750 | FINAL TUBE | 0 | INITIAL TUBE | 0 | LOSS OR GAIN | 0 | START CASE | 750 |
| Channel Test | Test Date | CBL | 3/28/2011 |
|
|
|
|
|