Form 21 | Related Doc |
Date Submitted: | 12/16/2009 | MIT Assigned By: | KOEHLER, BOB |
Date Recv'd: | 12/18/2009 | API number: | 05-103-09190 |
DocNum: | 1769888 | Facility Status: | AC |
Operator Information: |
Oper. No. | 16700 |
Operator: | CHEVRON U S A INC |
Address: | 6001 BOLLINGER CANYON RD SAN RAMON CA 94583 |
Type Of Facility: | WELL | Well Status: AC |
Well Name/No. | UNION PACIFIC |
Operator contact: | DIANE L PETERSON |
Location: | | qtrqtr: SENW | section: 28 | township: 2N | range: 102W | meridian: 6 |
|
MIT Details: |
Test Type: | VERIFICATION OF REPAIRS |
Repair Type: | TUBING/PACKER LEAK |
Repair Desc: | Shut in producing well - UIC failure - replace 184 joints 2 7/8" tubing DYB fiberlined tubing. |
Test Date: | 12/15/2009 |
Field Rep: | |
Approved Date: | 12/30/2009 |
Approved by: | KOEHLER, BOB |
Last Approved MIT: | 9/27/2004 |
Injection/Producing Formation Zones: | WEBR |
Perforation Interval: | 5744-6440 |
Open Hole Interval: | NA |
Bridge/Cement Plug Depth: | NA |
Tubing Size: | 2.875 |
Tubing Depth: | 5558 |
Top Packer Depth: | 5522 |
Multiple Packers: | N |
|
Condition of approval: |
|
Test Data: | Wellbore Channel Test: | Reading Type | Pressure | 10 MIN CASE | | 5 MIN CASE | | CASE BEFORE | | FINAL CASE | 800 | FINAL TUBE | | INITIAL TUBE | | LOSS OR GAIN | -20 | START CASE | 820 |
| No channel test. |
|
|
|
|