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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-07426UNION PACIFIC
78X-21
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
7/15/2019
RANGELY
72370
RIO BLANCO  103
SWSE 21 2N102W 6
314857View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:9/11/2007MIT Assigned By:KING, KEVIN
Date Recv'd:3/17/2008Facility ID: 150200
DocNum:1260485Facility Status:AC
Operator Information:
Oper. No.16700
Operator:CHEVRON U S A INC
Address:6001 BOLLINGER CANYON RD  SAN RAMON  CA 94583
Type Of Facility:UIC ENHANCED RECOVERYWell Status: AC
Facility NameUNION PACIFIC
Operator contact:DIANE  PETERSON
Location:  qtrqtr: SENE section: 16 township: 2N range: 103W meridian: 6
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:CASING LEAK
Repair Desc:Fish packer, clean out to 6458, run 5 1/2 liner from surface to 6465', perforate casing, acidize.
Test Date:9/10/2007
Field Rep:
Approved Date:3/17/2008
Approved by:KING, KEVIN
Last Approved MIT:5/7/2003
Injection/Producing Formation Zones:WEBR
Perforation Interval:6120 -6237
Open Hole Interval:NA
Bridge/Cement Plug Depth:
Tubing Size:2.875
Tubing Depth:6104
Top Packer Depth:6041
Multiple Packers:Y
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE
5 MIN CASE
CASE BEFORE
FINAL CASE805
FINAL TUBE
INITIAL TUBE
LOSS OR GAIN0
START CASE805
Channel TestTest Date
CBL 8/30/2007