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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-07426UNION PACIFIC
78X-21
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
7/15/2019
RANGELY
72370
RIO BLANCO  103
SWSE 21 2N102W 6
314857View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:1/15/2015MIT Assigned By:Browning, Chuck
Date Recv'd:1/15/2015Facility ID: 150200
DocNum:1171750Facility Status:AC
Operator Information:
Oper. No.16700
Operator:CHEVRON PRODUCTION COMPANY
Address:100 CHEVRON RD  RANGELY  CO 81648
Type Of Facility:UIC ENHANCED RECOVERYWell Status: AC
Facility NameUNION PACIFIC
Operator contact:DIANE  PETERSON
Location:  qtrqtr: SENE section: 16 township: 2N range: 103W meridian: 6
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:TUBING/PACKER LEAK
Repair Desc:FISH PACKERS, ADD ADDITIONAL PERF IN WEBER FORMATION, RIH WITH 188 JTS NEW FIBERLINED TUBING
Test Date:1/15/2015
Field Rep:Browning, Chuck
Approved Date:1/15/2015
Approved by:Browning, Chuck
Last Approved MIT:8/27/2012
Injection/Producing Formation Zones:WEBR
Perforation Interval:6120-6477
Open Hole Interval:NA
Bridge/Cement Plug Depth:NA
Tubing Size:2.875
Tubing Depth:6309
Top Packer Depth:6045.2
Multiple Packers:N
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE1250
5 MIN CASE1250
CASE BEFORE0
FINAL CASE1250
FINAL TUBE0
INITIAL TUBE0
LOSS OR GAIN0
START CASE1250
No channel test.