Form 21 | Related Doc |
Date Submitted: | 9/9/2004 | MIT Assigned By: | KRABACHER, JAY |
Date Recv'd: | 10/8/2004 | Facility ID: | 150200 |
DocNum: | 1170670 | Facility Status: | AC |
Operator Information: |
Oper. No. | 16700 |
Operator: | CHEVRON PRODUCTION COMPANY |
Address: | 100 CHEVRON RD RANGELY CO 81648 |
Type Of Facility: | UIC ENHANCED RECOVERY | Well Status: AC |
Facility Name | UNION PACIFIC |
Operator contact: | DIANE PETERSON |
Location: | | qtrqtr: SENE | section: 16 | township: 2N | range: 103W | meridian: 6 |
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MIT Details: |
Test Type: | VERIFICATION OF REPAIRS |
Repair Type: | CASING LEAK |
Repair Desc: | isolate and cement CSG leak. replace 170 jts tubing |
Test Date: | 9/8/2004 |
Field Rep: | |
Approved Date: | 10/8/2004 |
Approved by: | KRABACHER, JAY |
Last Approved MIT: | 9/30/1999 |
Injection/Producing Formation Zones: | WEBR |
Perforation Interval: | 5637 - 6282 |
Open Hole Interval: | NA |
Bridge/Cement Plug Depth: | |
Tubing Size: | 2.875 |
Tubing Depth: | 5411 |
Top Packer Depth: | 5275 |
Multiple Packers: | N |
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Condition of approval: |
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Test Data: | Wellbore Channel Test: | Reading Type | Pressure | 10 MIN CASE | 770 | 5 MIN CASE | 795 | CASE BEFORE | 0 | FINAL CASE | 755 | FINAL TUBE | 0 | INITIAL TUBE | 0 | LOSS OR GAIN | -50 | START CASE | 805 |
| No channel test. |
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