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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-07598SHARPLES-MCLAUGHLIN
12X33
SCOUT ENERGY MANAGEMENT LLC
10779
PR
5/1/2017
RANGELY
72370
RIO BLANCO  103
NESE 33 2N102W 6
314947View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:N/AMIT Assigned By:KRABACHER, JAY
Date Recv'd:9/21/2004Facility ID: 150200
DocNum:1170607Facility Status:AC
Operator Information:
Oper. No.16700
Operator:CHEVRON PRODUCTION COMPANY
Address:100 CHEVRON RD  RANGELY  CO 81648
Type Of Facility:UIC ENHANCED RECOVERYWell Status: AC
Facility NameSHARPLES-MCLAUGHLIN
Operator contact:DIANE  PETERSON
Location:  qtrqtr: SENE section: 16 township: 2N range: 103W meridian: 6
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:OTHER
Repair Desc:well failed routine UIC check.
Test Date:5/14/2004
Field Rep:
Approved Date:9/21/2004
Approved by:KRABACHER, JAY
Last Approved MIT:5/6/2003
Injection/Producing Formation Zones:WEBR
Perforation Interval:5571 - 6386
Open Hole Interval:NA
Bridge/Cement Plug Depth:
Tubing Size:2.875
Tubing Depth:5337
Top Packer Depth:5269
Multiple Packers:N
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE795
5 MIN CASE800
CASE BEFORE0
FINAL CASE795
FINAL TUBE0
INITIAL TUBE0
LOSS OR GAIN-5
START CASE800
No channel test.