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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-07537CARNEY C T
29 X 34
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
1/1/2024
RANGELY
72370
RIO BLANCO  103
NWSE 34 2N102W 6
314912View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:1/17/2024MIT Assigned By:
Date Recv'd:1/17/2024Facility ID: 
DocNum:403657580Facility Status:
Operator Information:
Oper. No.10779
Operator:SCOUT ENERGY MANAGEMENT LLC
Address:13800 MONTFORT DRIVE SUITE 100  DALLAS  TX 75240
Type Of Facility:Well Status: 
Facility NameCARNEY C T
Operator contact:Anita  Sanford
Location:  qtrqtr:  section:  township:  range:  meridian: 
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:
Repair Desc:Casing leak found from 3526'-3801'. TOC was at 3850'. Made decision to circulate cement through leak all the way to surface. Pumped 370 sks 13.4#/1.61 yield premium G cmt and got returns to surface. Clean out cement and CICR and chart test casing to 1250 psi - Passed rig test. RIH w/ injection equipment. Return to injection pending an approved Form 21.
Test Date:1/15/2024
Field Rep:Browning, Chuck
Approved Date:1/17/2024
Approved by:
Last Approved MIT:9/26/2018
Injection/Producing Formation Zones:WEBR
Perforation Interval:5630-6338
Open Hole Interval:
Bridge/Cement Plug Depth:
Tubing Size:2.875
Tubing Depth:5977
Top Packer Depth:5345
Multiple Packers:
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE1350
5 MIN CASE1355
FINAL CASE1350
LOSS OR GAIN-10
START CASE1360
No channel test.