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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-07978LACY, S B
7X
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
8/1/2023
RANGELY
72370
RIO BLANCO  103
NWSW 24 2N103W 6
315138View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:8/29/2023MIT Assigned By:
Date Recv'd:8/29/2023Facility ID: 
DocNum:403511413Facility Status:
Operator Information:
Oper. No.10779
Operator:SCOUT ENERGY MANAGEMENT LLC
Address:13800 MONTFORT DRIVE SUITE 100  DALLAS  TX 75240
Type Of Facility:Well Status: 
Facility NameLACY, S B
Operator contact:Anita  Sanford
Location:  qtrqtr:  section:  township:  range:  meridian: 
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:
Repair Desc:"8/23 UIC Repair - CO well down to 6496' (bad casing from 6246-6496. Isolated casing leak from 4011' - 4043'). Squeezed w/ 15.8# class G cmt (50 sxs prepared, 44.9 sxs behind casing a 5.1 sxs in wellbore, DO cmt, still leaking. Squeezed w/ 300 psi seal maker (65 total gals), still leaking. Final squeeze attempt was w/ 13.4# fine cmt, mixed 15 sxs total (3.8 sxs behind casing rest in wellbore, DO slowly with no more than 4k on bit. casing tested - good. "
Test Date:8/24/2023
Field Rep:Browning, Chuck
Approved Date:8/31/2023
Approved by:
Last Approved MIT:6/6/2018
Injection/Producing Formation Zones:WEBR
Perforation Interval:5960-6580
Open Hole Interval:
Bridge/Cement Plug Depth:
Tubing Size:2.875
Tubing Depth:0
Top Packer Depth:0
Multiple Packers:
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE1240
5 MIN CASE1260
FINAL CASE1240
LOSS OR GAIN-60
START CASE1300
No channel test.