Form 21 | Related Doc |
Date Submitted: | 8/29/2023 | MIT Assigned By: | |
Date Recv'd: | 8/29/2023 | Facility ID: | |
DocNum: | 403511413 | Facility Status: | |
Operator Information: |
Oper. No. | 10779 |
Operator: | SCOUT ENERGY MANAGEMENT LLC |
Address: | 13800 MONTFORT DRIVE SUITE 100 DALLAS TX 75240 |
Type Of Facility: | | Well Status: |
Facility Name | LACY, S B |
Operator contact: | Anita Sanford |
Location: | | qtrqtr: | section: | township: | range: | meridian: |
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MIT Details: |
Test Type: | VERIFICATION OF REPAIRS |
Repair Type: | |
Repair Desc: | "8/23 UIC Repair - CO well down to 6496' (bad casing from 6246-6496. Isolated casing leak from 4011' - 4043').
Squeezed w/ 15.8# class G cmt (50 sxs prepared, 44.9 sxs behind casing a 5.1 sxs in wellbore, DO cmt, still leaking.
Squeezed w/ 300 psi seal maker (65 total gals), still leaking.
Final squeeze attempt was w/ 13.4# fine cmt, mixed 15 sxs total (3.8 sxs behind casing rest in wellbore, DO slowly with no more than 4k on bit. casing tested - good. "
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Test Date: | 8/24/2023 |
Field Rep: | Browning, Chuck |
Approved Date: | 8/31/2023 |
Approved by: | |
Last Approved MIT: | 6/6/2018 |
Injection/Producing Formation Zones: | WEBR |
Perforation Interval: | 5960-6580 |
Open Hole Interval: | |
Bridge/Cement Plug Depth: | |
Tubing Size: | 2.875 |
Tubing Depth: | 0 |
Top Packer Depth: | 0 |
Multiple Packers: | |
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Condition of approval: |
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Test Data: | Wellbore Channel Test: | Reading Type | Pressure | 10 MIN CASE | 1240 | 5 MIN CASE | 1260 | FINAL CASE | 1240 | LOSS OR GAIN | -60 | START CASE | 1300 |
| No channel test. |
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