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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-09197GRAY
A-8AX
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
8/1/2023
RANGELY
72370
RIO BLANCO  103
SESE 24 2N103W 6
315767View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:8/13/2018MIT Assigned By:
Date Recv'd:8/13/2018Facility ID: 
DocNum:401731488Facility Status:
Operator Information:
Oper. No.16700
Operator:CHEVRON USA INC
Address:100 CHEVRON RD  RANGELY  CO 81648
Type Of Facility:Well Status: 
Facility NameGRAY
Operator contact:DIANE  PETERSON
Location:  qtrqtr:  section:  township:  range:  meridian: 
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:
Repair Desc:WELLWORK TO REPAIR CASING LEAK. ISOLATED CASING LEAK AT 3786-3830SQUEEZE LEAK WITH 3 BBLS 300PSI PRODUCTION PRESSURE TO 1400PSI.
Test Date:8/10/2018
Field Rep:Browning, Chuck
Approved Date:8/15/2018
Approved by:
Last Approved MIT:5/5/2017
Injection/Producing Formation Zones:WEBR
Perforation Interval:5802-6500
Open Hole Interval:
Bridge/Cement Plug Depth:
Tubing Size:2.875
Tubing Depth:5746.4
Top Packer Depth:5649.4
Multiple Packers:
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE1240
5 MIN CASE1240
FINAL CASE1240
START CASE1240
No channel test.