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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-05757HAGOOD L N
A-7
SCOUT ENERGY MANAGEMENT LLC
10779
AC
3/1/2023
RANGELY
72370
RIO BLANCO  103
NWNE 23 2N103W 6
314462View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:6/17/2016MIT Assigned By:
Date Recv'd:6/17/2016Facility ID: 
DocNum:401064383Facility Status:
Operator Information:
Oper. No.16700
Operator:CHEVRON USA INC
Address:100 CHEVRON RD  RANGELY  CO 81648
Type Of Facility:Well Status: 
Facility NameHAGOOD L N
Operator contact:DIANE  PETERSON
Location:  qtrqtr:  section:  township:  range:  meridian: 
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:
Repair Desc:REPAIR WELLHEAD - SQUEEZE LEAK BETWEEN 7" AND 9 5/8" CASING. RAN IN HOLE WITH NEW PACKER AND TUBING. CORRECTED PERFORATION INTERVAL
Test Date:6/15/2016
Field Rep:Browning, Chuck
Approved Date:6/17/2016
Approved by:
Last Approved MIT:3/16/2012
Injection/Producing Formation Zones:WEBR
Perforation Interval:6126-6592
Open Hole Interval:
Bridge/Cement Plug Depth:
Tubing Size:2.875
Tubing Depth:6073.2
Top Packer Depth:5916
Multiple Packers:
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE1200
5 MIN CASE1200
FINAL CASE1200
START CASE1200
No channel test.