Skip to Main Content

Incident Search

COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-05811GRAY
B-8
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
11/22/2021
RANGELY
72370
RIO BLANCO  103
SENE 13 2N103W 6
314485View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:12/10/2015MIT Assigned By:
Date Recv'd:12/10/2015Facility ID: 
DocNum:400951259Facility Status:
Operator Information:
Oper. No.16700
Operator:CHEVRON PRODUCTION COMPANY
Address:100 CHEVRON RD  RANGELY  CO 81648
Type Of Facility:Well Status: 
Facility NameGRAY
Operator contact:DIANE  PETERSON
Location:  qtrqtr:  section:  township:  range:  meridian: 
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:
Repair Desc:CEMENT SQUEEZE CASING LEAK, RUN 5 1/2" LINER FROM SURFACE TO 6324'. RUN NEW 2 7/8" FIBER LINED TUBING AND PACKER
Test Date:12/10/2015
Field Rep:Browning, Chuck
Approved Date:12/10/2015
Approved by:
Last Approved MIT:4/11/2011
Injection/Producing Formation Zones:WEBR
Perforation Interval:
Open Hole Interval:6360-6537
Bridge/Cement Plug Depth:
Tubing Size:2.875
Tubing Depth:6337.3
Top Packer Depth:6262
Multiple Packers:
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE1205
5 MIN CASE1205
FINAL CASE1205
START CASE1205
No channel test.