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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-07155MB LARSON GOV
C9 X 25
SCOUT ENERGY MANAGEMENT LLC
10779
PR
5/1/2022
RANGELY
72370
RIO BLANCO  103
SESW 25 2N102W 6
314760View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:12/7/2015MIT Assigned By:
Date Recv'd:12/7/2015Facility ID: 
DocNum:400949174Facility Status:
Operator Information:
Oper. No.16700
Operator:CHEVRON PRODUCTION COMPANY
Address:100 CHEVRON RD  RANGELY  CO 81648
Type Of Facility:Well Status: 
Facility NameMB LARSON GOV
Operator contact:DIANE  PETERSON
Location:  qtrqtr:  section:  township:  range:  meridian: 
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:
Repair Desc:RUN 192 JOINTS TK2 2 7/8" TUBING AND PACKER
Test Date:12/3/2015
Field Rep:Granahan, Kyle
Approved Date:12/8/2015
Approved by:
Last Approved MIT:N/A
Injection/Producing Formation Zones:WEBR
Perforation Interval:6118-6480
Open Hole Interval:
Bridge/Cement Plug Depth:
Tubing Size:2.875
Tubing Depth:6034.1
Top Packer Depth:6029.7
Multiple Packers:
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE400
5 MIN CASE400
FINAL CASE400
START CASE400
No channel test.