Skip to Main Content

Incident Search

COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-06159UNION PACIFIC
47-21
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
1/31/2023
RANGELY
72370
RIO BLANCO  103
NWNW 21 2N102W 6
314584View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:8/27/2015MIT Assigned By:
Date Recv'd:8/27/2015Facility ID: 
DocNum:400890971Facility Status:
Operator Information:
Oper. No.16700
Operator:CHEVRON PRODUCTION COMPANY
Address:100 CHEVRON RD  RANGELY  CO 81648
Type Of Facility:Well Status: 
Facility NameUNION PACIFIC
Operator contact:DIANE  PETERSON
Location:  qtrqtr:  section:  township:  range:  meridian: 
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:
Repair Desc:Replace 187 joints 2 7/8" fiberlined tubing and packer, corrective action document #668403131. Bottom liner 6065-6593' - Packer depth approval referance COGCC document #2597162 (100' bottom liner top).
Test Date:8/26/2015
Field Rep:Browning, Chuck
Approved Date:10/13/2015
Approved by:
Last Approved MIT:1/26/2011
Injection/Producing Formation Zones:WEBR
Perforation Interval:6222-6300
Open Hole Interval:
Bridge/Cement Plug Depth:
Tubing Size:2.875
Tubing Depth:6193.3
Top Packer Depth:5992.2
Multiple Packers:
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE1250
5 MIN CASE1250
FINAL CASE1250
LOSS OR GAIN-2
START CASE1250
No channel test.