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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-05655NEAL
4
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
1/27/2023
RANGELY
72370
RIO BLANCO  103
SENW 25 2N103W 6
314412View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:8/27/2015MIT Assigned By:
Date Recv'd:8/27/2015Facility ID: 
DocNum:400890955Facility Status:
Operator Information:
Oper. No.16700
Operator:CHEVRON PRODUCTION COMPANY
Address:100 CHEVRON RD  RANGELY  CO 81648
Type Of Facility:Well Status: 
Facility NameNEAL
Operator contact:DIANE  PETERSON
Location:  qtrqtr:  section:  township:  range:  meridian: 
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:
Repair Desc:Clean out wellbore, run in hole with 168 joints new fiberlined tubing and packer. Correct perforation interval 6103-6452 - Form 5A doc #400883968
Test Date:8/26/2015
Field Rep:Browning, Chuck
Approved Date:9/29/2015
Approved by:
Last Approved MIT:1/28/2013
Injection/Producing Formation Zones:WEBR
Perforation Interval:6103-6452
Open Hole Interval:
Bridge/Cement Plug Depth:
Tubing Size:2.875
Tubing Depth:6103.6
Top Packer Depth:6029.1
Multiple Packers:
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE1250
5 MIN CASE1250
FINAL CASE1250
START CASE1250
No channel test.