Form 21 | Related Doc | Date Submitted: | 4/25/2013 | MIT Assigned By: | QUINT, CRAIG | Date Recv'd: | 4/26/2013 | Facility ID: | 159260 | DocNum: | 2561148 | Facility Status: | CL | Operator Information: | Oper. No. | 10399 | Operator: | NIGHTHAWK PRODUCTION LLC | Address: | 1805 SHEA CENTER DR #290 HIGHLANDS RANCH CO 80129 | Type Of Facility: | UIC DISPOSAL | Well Status: CL | Facility Name | JOLLY RANCH | Operator contact: | BILL MCKNAB | Location: | | qtrqtr: NWSE | section: 1 | township: 13S | range: 56W | meridian: 6 |
| MIT Details: | Test Type: | VERIFICATION OF REPAIRS | Repair Type: | OTHER | Repair Desc: | CHANGED OUT TUBING BECAUSE OF BAD LINING. | Test Date: | 4/25/2013 | Field Rep: | QUINT, CRAIG | Approved Date: | 4/26/2013 | Approved by: | QUINT, CRAIG | Last Approved MIT: | 5/7/2012 | Injection/Producing Formation Zones: | ABCK | Perforation Interval: | 8090 - 8194 | Open Hole Interval: | NA | Bridge/Cement Plug Depth: | NA | Tubing Size: | 2.375 | Tubing Depth: | 8048 | Top Packer Depth: | 8048 | Multiple Packers: | N | | Condition of approval: | | Test Data: | Wellbore Channel Test: | Reading Type | Pressure | 10 MIN CASE | 820 | 5 MIN CASE | 820 | CASE BEFORE | 0 | FINAL CASE | 820 | FINAL TUBE | 0 | INITIAL TUBE | 0 | LOSS OR GAIN | 0 | START CASE | 820 |
| No channel test. |
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