Skip to Main Content

Incident Search

COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-01032CARNEY
17-35
SCOUT ENERGY MANAGEMENT LLC
10779
SI
7/1/2024
RANGELY
72370
RIO BLANCO  103
SWNW 35 2N102W 6
314244View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:2/14/2012MIT Assigned By:KOEHLER, BOB
Date Recv'd:2/16/2012API number: 05-103-01032
DocNum:1771703Facility Status:SI
Operator Information:
Oper. No.16700
Operator:CHEVRON USA INC
Address:100 CHEVRON ROAD  RANGELY  CO 81648
Type Of Facility:WELLWell Status: SI
Well Name/No.CARNEY
Operator contact:DIANE L.  PETERSON
Location:  qtrqtr: SWNW section: 35 township: 2N range: 102W meridian: 6
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:TUBING/PACKER LEAK
Repair Desc:Carney 17-35 was a shut in production well, replaced tubing and packer.
Test Date:2/9/2012
Field Rep:
Approved Date:2/22/2012
Approved by:KOEHLER, BOB
Last Approved MIT:N/A
Injection/Producing Formation Zones:WEBR
Perforation Interval:5704-6414
Open Hole Interval:NA
Bridge/Cement Plug Depth:NA
Tubing Size:2.875
Tubing Depth:5354
Top Packer Depth:5255
Multiple Packers:N
 
Condition of approval:
Email from Diane Peterson to Bob Koehler. Tubing and packer leaks repaired by replacing them. This MIT meant to test new packer and tubing. Well returned to production on 2/19/2012. Gap between Top Packer and Top Perf is OK in this situation.
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE
5 MIN CASE
CASE BEFORE
FINAL CASE525
FINAL TUBE
INITIAL TUBE
LOSS OR GAIN0
START CASE525
No channel test.